Term
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Definition
Purpose: To provide the instructions necessary to vary plant load from 20-100% power, determine the rate of power ascension, and establish steady state operation.
Operational Mode: Mode 1 is defined as Keff³0.99, thermal power >5% and TAVG³350°F.
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Term
IOP Precaustions and Limitations: |
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Definition
When > P-2 {PT-505 > 15%, 1oo1, enables auto rod withdrawal}, auto rod control should be maintained except for adjustments to AFD, load changes, or IAW approved procedures.
- Compare NI power to DT for detection of miscalibration of the NIs.
- With Feedwater Crossflow valid correction factor:
Average power level over a 1 hour period should not exceed 100% (3459 MWt)
- Without Feedwater Crossflow valid correction factor:
Average power level over a 1 hour period should not exceed 98.6% (3411 MWt)
- Another CP bed must be put in service every 20%.
- If Thermal Power change exceeds 15% of RTP within 1 hr period, then inform chemistry to obtain RCS samples between 2-6 hrs. (R16 and R41 readings required.)
- Operation without Crossflow (or with an invalid CF) shall not exceed 24 hours; if unavailable > 20 hours, restore with a valid CF within 4 hrs, or lower power < 98.6% within that 4 hours.
To prevent adjusting power into an overpower condition, the following rules are to be adhered to:
· The NCO willensure PT505, PT506, and Average ΔT Power do NOT exceed the values specified in S2.RE‑RA.ZZ‑0011, Tables (these parameters are NOT affected by feedwater nozzle fouling). A +0.3°F tolerance for ΔT and +3.5 psia tolerance for PT505/PT506 is allowed, which corresponds to 0.5% power.
· The CRS is aware that the following are known to cause defouling of the feedwater nozzles.
· Notification from Chemistry of Feedwater/Condensate chemistry transients including ph, oxygen, iron, and chemical treatment.
· Reactor power change of >5% from full power.
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Term
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Definition
TS 3.4.9: RCS specific activity is limited to £1.0mCi/gm and £100/E mCi/gm. An isotopic analysis for Iodine including I-131, I-133, & I-135 2-6 hours following a power change exceeding 15% in one hour. Basis: Limits ensure that the 2 hour dose at the site boundary will not exceed a small fraction of the Part100 limits. The 2-6 hour requirement is based on the detection and collection of data concerning Iodine spiking.
TS 3.3.1.1: Calorimetric required at least once per 24 hrs when >15% RTP. At least one calorimetric must be performed between 50-90% RTP. Basis: Ensure PRNI accurate within 2% at 100% RTP.
TS 3.1.1.4: Maintain temperature greater than minimum temperature for criticality (≥541°F). Bases: This limitation ensures: (1) MTC is within analyzed range, (2) protective instrumentation within normal operating range, (3) the P-12 {Tave < 543°F, 2oo4, Allows manual block of HI Steam Flow SI, Enables Group I Steam Dumps} interlock above allowable setpoint, (4) PZR is capable of being operable with a steam bubble, and (5) pressure vessel above minimum RTNDT temperature.
Power ascension limits: Limits are imposed to prevent the adverse effects of pellet – clad interaction (PCI). This is of great concern following refueling since handling of the fuel could cause some pellet misalignment and possible clad contact.
- Control rod motion should be minimized during the post-refueling startup. When >50% power the withdrawal rate is limited to 3 %/hour for heights at which the rods have not been previously positioned (post-refueling).
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Term
Equipment Operation During Ascension: |
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Definition
Start with:
- Group busses transferred
- 2 CN pumps in service, 1 SGFP in service
Equipment Operation During Ascension:
- >20% turbine load - place BSCDT pumps in service
- 25-30% reactor power - shut MS7s
- Prior to 40% - evaluate MSR auto operation
- >40% reactor power - place second SGFP in service
· ³40% turbine load - ensure A-36: AMSAC BYPASSED alarm clear, begin heater drain pump cleanup
- prior to exceeding 50% - perform AFD & QPTR calculations
- >50% - place HDPs in service
- ³70% - verify SGFP runback armed
- ³75% - start third condensate pump
- < 89.5% - ensure PT.TRB-0003 performed
- < 90% - reevaluate MSRs, Calorimetric if not yet performed
- 98 - 98.6% - verify Feedwater Crossflow System
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Term
Equipment Operation During Downpower: |
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Definition
- Rapid load reductions, ≥5%/min, require use of AB.LOAD-0001
- Transfer Group Busses
- Stabilize <20% Rx power and go to IOP-5
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Term
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Definition
- Set EHC setter to 66% and
- VLV POS CNTRL ramp rate to 15%/minute
- TURB INLET PRESS CNTRL ramp rate to 15%/minute
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Term
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Definition
Allows operation above 98.6% 3411MWt
3hrs 20 mins to of data collection > 85% for valid Correction Factor before assending to 3411
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Term
Fuel Conditioning / Ramp Rates (NF-AP-440)
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Definition
Not fully Conditioned:
0-40% - no limits
40-72% - 3% per hour
72-100% - .5% per hour
Fully Conditioned: operated at that power level or higher for a total of 72 hours within a 7-day period
0-40% - no limits
40-72% - 3% per hour
72-90% - 2% per hour
90-100% - 1% per hour
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